Hello,
Yanmar2qm15.
Screen shot from a video i was filming with my
phone. Ill see if i can upload that as well.
So the original Morse throttle/shifter had an internal piece snap. Long story short, is that i replaced it with a dometic side mounted controller.
I put in new
cables. Then I started up the
engine to see how it idled and what not. It seemed to be going pretty well. I had noticed a new leak in the lazarette where the inside half of the new controller is located. Figured I'd look into that later.
So its running smoothly, its spurting
water out the stern regularly and the same amount that I've ever seen. I decide to rev it up and take a look at the connections. I was taking a video when the
raw water hose burst at the
engine block connection (shown above).
My theory right now is that leak from before was because I possibly cracked the (very) old hose from the inside while farting around installing the new controller. Which caused the sleeve to fill up and burst.
However, my worry is that there is back pressure building up for some reason? Maybe, its because i set the throttle settings at the choke incorrectly?
I have new 200psi (not
steel reinf.) red rubber hose and im hoping make sure that im not just going to blow up another hose.
I look forward to your responses.
Thanks,
AB
P.S. ill try and upload the video as well.